White's '95 GT "Unicorn"

Tony

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Fancy!!!!
 

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white95

white95

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Started the KRC PS pump install. Had to remove the radiator fan, RH tensioner and belt. I’m going to have to run a stretch fit belt for the AC but I’m seriously considering just yanking it.

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The kit was very straightforward to install.

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This was the moment when I realized I should’ve put the other belt on first. Then the phone rang and I have to go back to work.
 
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white95

white95

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Howdy! :) I think Whitey has beaten you for the longest lasting build thread on the internet hahaa!

Everyone deserves a good role model :cool:

and your challenging the largest # of builds. Are you going to share the latest here?

That ain’t no shit!!

Idk man, I think I'm starting to catch him lmfao

But one area he absolutely has me beat is in progress made. Holy ballz Yoooosef!

I’ve been busy man! My IG doesn’t show the nitty gritty details of the crap I’ve gone through with this MF!! So much left to do!!

Stay tuned :cool:
 
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white95

white95

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Finally got back to the new PS system installation and I’ve all but finished it.

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Started by using the electric setup to pump as much of Pentosin out as possible.

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I’m almost disappointed that it worked as planned and didn’t make a huge mess. Finished up by making a new high pressure hose and tying the return lines together. Filled the reservoir and fired it up!!

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Didn’t get footage of the fluid puking everywhere or the look on my face when the bolts backed out of the WP pulley. It made a huge mess after all.

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Sigh… Time to drink beer… I’ll get back to this Sunday!

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white95

white95

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Today’s resumption of work will include the installation of a front brake cooling setup. Big thanks to @ReplicaR for donating an extra set of inlet ducts to the cause. These will be pop-riveted in place in the outboard inlet. I’m also going to ditch the mesh screens.

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ttocs

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you would be amazed how much the mesh can cut down on airflow. When I was in AZ I had an RC airplane field 100 yrds from my house and I started to fly there. At the time the electrically ducted fans/jets were becoming popular and a lot of the guys were flying them as they were fast and loud. One problem we had with them is that the field we flew off of had a decomposed granite runway and while they were taking off they would suck small rocks into the ducts and tear up the fans. A couple of guys put some mesh on the front of the ducts and then were amazed to find that with almost any mesh in front of the ducts that they had problems going fast enough to even take off.
 
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white95

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Finished the KRC installation and hit the road for a test drive. My initial impression was how much smoother and linear the steering response is now. Now, making rapid left and right maneuvers along with braking while turning are now a non-issue. I need to bleed the hydroboost for it to be perfect but I’m am very hopeful.

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white95

white95

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Installed anti-rattle clips on the rear pads.

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Adjusted the panhard bar to center the rear.

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In the middle of installing the five point harness.

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Now running out to get a new windshield strip.
 

Hans

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Re: my SECOND build thread
Pictures from 2006-2008

The pictures Josh texted me when I enquired about the car in the summer of 2006.

36359226374_60ec59942b_t.jpgImage286229 by oldawgnewtrikz, on Flickr

36359226384_94a511b32d_t.jpgImage286129 by oldawgnewtrikz, on Flickr

36359226284_1e279de9bf_t.jpgImage286629 by oldawgnewtrikz, on Flickr

After we installed the 2" lowering coils, I snapped this picture with a potato.

36359223454_f6abcc15b9_t.jpgmustang by oldawgnewtrikz, on Flickr

Installed a black S-351 wing, which wasn't in the greatest shape and flew off the car. I think.

36382292193_6bd32433ec_n.jpgProject Unicorn by oldawgnewtrikz, on Flickr

36382291843_8d9178752a_n.jpgProject Unicorn by oldawgnewtrikz, on Flickr

36382291773_3bd6f08b7e_n.jpgProject Unicorn by oldawgnewtrikz, on Flickr

36382291693_7a49f92bfa_n.jpgProject Unicorn by oldawgnewtrikz, on Flickr

36382291943_b18081ceb0_n.jpgProject Unicorn by oldawgnewtrikz, on Flickr

36382292033_1a820dfe87_n.jpgProject Unicorn by oldawgnewtrikz, on Flickr

E303 cam swap

37196174205_54127b5a63_c.jpgProject Unicorn by oldawgnewtrikz, on Flickr

36359227164_7d578de762_z.jpgImage57 by oldawgnewtrikz, on Flickr

Installed a flip out navigation, DVD screen. Look at that Porno red interior!! Sometimes I wish I had left that alone.

37005842086_e5981580ce_c.jpgProject Unicorn by oldawgnewtrikz, on Flickr

36359039274_154d05b766_n.jpgProject Unicorn by oldawgnewtrikz, on Flickr

36359039154_6803fe331f_c.jpgProject Unicorn by oldawgnewtrikz, on Flickr

Saved up and bought some Konig Maxxim wheels.

36359227524_1faa46607d_z.jpgImage05 by oldawgnewtrikz, on Flickr

36359227494_fc69f336c2_z.jpgImage07 by oldawgnewtrikz, on Flickr

36359227324_41aee4c814_z.jpgImage12 by oldawgnewtrikz, on Flickr

36359227254_8cc40bb749_z.jpgImage13 by oldawgnewtrikz, on Flickr

Had a leaky rear main seal and pressure washed the undercarriage. We hit the easy button.

36359227214_78411d5508_z.jpgImage40 by oldawgnewtrikz, on Flickr
Is that a Hyster?
 
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white95

white95

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What a week.. Took off yesterday to finalize a few things on the car prior to a third party tech inspection. Finally added the line to the coolant over flow tank, washed the car and set out to the inspector. Noticed a little water in the floor board but passed it off as wet shoes.

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The car passed inspection without any concerns!! Before I headed home, I decided to wipe the water up and quickly realized it was a petroleum based fluid. Power steering fluid.

Fuck.

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Didn’t notice anything obvious so I headed home. Half way home, I noticed a few drops on my shoe and I truly became concerned. This is just my luck.

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It’s leaking from the seal on the other side of this boot where the piston rod attached to the booster unit.

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Demoralized but undeterred, I’ve scoured the internet for a replacement. Several calls to Mustang recyclers later, I found little hope.

However… I found on locally at Advance Auto Parts and will scoop that up after picking my buddies trailer up after work.

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white95

white95

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As I arrived to retrieve the trailer, it was being hooked to a Silverado. As it turned out, the owners Suburban broke down. So, I waited there for a little over an hour to pick it up.

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Not a big deal. Helped them get the burb into the yard and set out for Advance Auto Parts to pick my new booster up….

Or so I thought.

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It wasn’t the right part and I was pretty bummed out. It was for a damn power stroke truck. Dejected, I drove home and drank a few beers. Found yet another booster at Vatozone and I will pick it up midday today.

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