Forums
New posts
Search forums
What's new
New posts
New media
New media comments
New profile posts
Latest activity
Media
New media
New comments
Search media
Members
Current visitors
New profile posts
Search profile posts
Log in
Register
What's new
Search
Search
Search titles only
By:
New posts
Search forums
Menu
Log in
Register
Install the app
Install
Forums
Multimedia & Entertainment
Build Ups & Projects
2003 Mach 1 "Restomod" Project BadMach
JavaScript is disabled. For a better experience, please enable JavaScript in your browser before proceeding.
You are using an out of date browser. It may not display this or other websites correctly.
You should upgrade or use an
alternative browser
.
Reply to thread
Message
<blockquote data-quote="Deceptive GT" data-source="post: 1502809" data-attributes="member: 20380"><p>[ATTACH=full]17931[/ATTACH][ATTACH=full]17931[/ATTACH]</p><p></p><p>Update on the Mach 1. I put the SOS Pod with the Speedhut EGT and Boost Gauge in the car so it is not sitting in the garage where my dumbass will possibly break it.</p><p></p><p>Yesterday I decided to put a few miles on the car, 5 to be exact and things did not go so well.</p><p></p><p>The car runs hard, no doubt, however I doubt I will put anymore miles on this engine. I have been seeing an issue every now and then where, at idle, the oil pressure gauge wigs out and falls to zero then goes right back to normal. I have not had any noise other than possible tensioner noise at startup so I figured it is just the shit Melling Timing Components.</p><p></p><p>I took the car to the local Detailer’s Garage to get a foam cannon and some other stuff. When I got there I notice the oil pressure at zero when at idle but as soon as I blipped the throttle it came back to normal and stayed. This time it concerned me but no noise still.</p><p></p><p>Went in to get the stuff and got back in the car there was a noise about 8 times which was on a consistent interval then went away and never came back. But, the oil pressure gauge kept dropping to zero at almost every stop but again, a slight blip in throttle would bring it back up.</p><p></p><p>The guy who built the engine is supposed to be somebody that the Saleen and Shelby guys go to for their modular builds. I don’t know who is to blame for this engine. It has 310 miles on the engine, dyno sheet shows decent power for a low compression NA engine, I am sure being a stroker helped that. But I cannot trust the engine at this point.</p><p></p><p>The good news is that I found the, what are said to be ported heads, are DB castings so I think the engine will get pulled sooner to use these heads instead of the AGs I have.</p><p></p><p>I think I am selling the Procharger P1SC-1H and bracket and getting a Vortech V1 Si.</p><p></p><p>I am goin to sell the BBK Catted X Pipe and Aluminum Mac Prochamber.</p><p></p><p>I need to get the crank pulley puller for the Coyote so I can finish taking it apart in preparation for it’s rebuild and install in the GT and then pull the Mach 1 in and start disassembly for the new engine since there is no point in driving it anymore and risking damage.</p></blockquote><p></p>
[QUOTE="Deceptive GT, post: 1502809, member: 20380"] [ATTACH type="full"]17931[/ATTACH][ATTACH type="full"]17931[/ATTACH] Update on the Mach 1. I put the SOS Pod with the Speedhut EGT and Boost Gauge in the car so it is not sitting in the garage where my dumbass will possibly break it. Yesterday I decided to put a few miles on the car, 5 to be exact and things did not go so well. The car runs hard, no doubt, however I doubt I will put anymore miles on this engine. I have been seeing an issue every now and then where, at idle, the oil pressure gauge wigs out and falls to zero then goes right back to normal. I have not had any noise other than possible tensioner noise at startup so I figured it is just the shit Melling Timing Components. I took the car to the local Detailer’s Garage to get a foam cannon and some other stuff. When I got there I notice the oil pressure at zero when at idle but as soon as I blipped the throttle it came back to normal and stayed. This time it concerned me but no noise still. Went in to get the stuff and got back in the car there was a noise about 8 times which was on a consistent interval then went away and never came back. But, the oil pressure gauge kept dropping to zero at almost every stop but again, a slight blip in throttle would bring it back up. The guy who built the engine is supposed to be somebody that the Saleen and Shelby guys go to for their modular builds. I don’t know who is to blame for this engine. It has 310 miles on the engine, dyno sheet shows decent power for a low compression NA engine, I am sure being a stroker helped that. But I cannot trust the engine at this point. The good news is that I found the, what are said to be ported heads, are DB castings so I think the engine will get pulled sooner to use these heads instead of the AGs I have. I think I am selling the Procharger P1SC-1H and bracket and getting a Vortech V1 Si. I am goin to sell the BBK Catted X Pipe and Aluminum Mac Prochamber. I need to get the crank pulley puller for the Coyote so I can finish taking it apart in preparation for it’s rebuild and install in the GT and then pull the Mach 1 in and start disassembly for the new engine since there is no point in driving it anymore and risking damage. [/QUOTE]
Insert quotes…
Verification
Post reply
Random media
Latest posts
Wheel and tire specs?
Latest: SsgDoc94
17 minutes ago
Suspension and Brakes
D
New Member from Canada
Latest: Drhoward
Today at 11:56 AM
New Member Introductions
96blak54 2001 Cobra
Latest: white95
Today at 11:27 AM
Build Ups & Projects
A
1995 crank but no start situation
Latest: Armand
Today at 10:19 AM
94-95 5.0 - Specific
Missing cover behind flywheel
Latest: 96blak54
Today at 9:19 AM
96-04 - 2V Specific
Share this page
Reddit
Pinterest
Tumblr
WhatsApp
Email
Share
Link
Forum statistics
Threads
78,556
Messages
1,536,158
Members
16,201
Latest member
jgib8795
Members online
shovel
badass98svt
Forums
Multimedia & Entertainment
Build Ups & Projects
2003 Mach 1 "Restomod" Project BadMach
Top