So after replacing the starter, I no longer had an issue. Soon after I got the starter, I also got another shipment I hadn't expected. I had order a Holley 7" Digital Dash over break that was on backorder (Holley products on backorder, who would have guessed) and it had actually got in early. So I ordered a mount for the cluster from Eddie (@eddiett2v on Instagram) at a good price and quality. Install was straight forward and easy.
I got the car running soon after that, but unfortunately within 10 minutes of run time one of the lifters began leaking down and I had to tear the car back apart to replace it. I used some spare SBF lifters I had as they were the same, just a different brand.
After helping restore a 2004 Mach 1 (I'll make a post about that soon) the owner offered to order me a Holley Hi Ram Intake for my motor and I couldn't say no. In preparation for the intake I started looking at the Holley Dual Sync. However, the more and more I thought about it, I decided it would be easier to spend a little more and go with a Holley 36-1 Crank Trigger and Cam Sync. This would be used with LS coils that I found in a junkyard for a whopping $40. I didn't really want to buy expensive valve covers or coil brackets so I decided to make my own.
By now it's the end of March and I was told the intake would be here within the second week of March. After multiple calls to my local speed shop, we decided it would be best to put on the old intake and drive the car until the intake manifold would be in. With that, I finished the car and got it running with the new ignition system. It cranks a little longer on start-up to sync the crank and cam signals but overall it is very seamless and a worthwhile upgrade.
As I prepared to take the car to SIU to enjoy a couple weeks with at school, I heard the all to familiar lifter knock. After checking lash over and over again, I decided to trailer it to school and take it to our vehicle lab to go more in-depth with it. After using a pressure transducer with an oscilloscope we were able to determine the camshaft lobe on cylinder 5 was in trouble. With a school event only a week away, I decided to overnight a roller cam, roller lifters, pushrods, and all gaskets necessary (at this point I was done with flat tappet camshafts). I ripped the motor out within a couple of hours with the help of some friends and started disassembling the motor. The camshaft had not only wiped a lobe but had eaten up a good chunk of the lifter as well.
After thoroughly cleaning the oil pan, we installed the new F-303 camshaft and Melling retro-fit roller lifters. Everything was going smoothly. Retimed the motor and changed the firing order in the PCM and it was ready for break-in. During break-in we heard a pop and I killed the motor. After pulling the valve cover, a rocker arm stud had snapped. After further inspection, we found that the pushrods were too long and all 16 had been bent (thanks to me hastily measuring them improperly). Unfortunately, I didn't make the event but after replacing all the pushrods with the proper length ones as well as all rocker arm studs, the car was ready to drive. I drove the car around for the remaining two weeks of school and enjoyed every second of it, other than the throttle cable occasionally coming out which I eventually fixed for good.
Now we are caught up to May and I'll post more updates tomorrow.