Gee, maybe that’s why!

Daryl

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Quick refresher and backstory: I replaced the MAF unit, sensor, plugs and wires. Car ran like shit. Come to find the following:
Grommet that holds sensor onto the port on the side of the CAI tubing is missing. One spark plug boot all but melted onto exhaust header pipe. Plus, 2 of the 8 new plugs were cracked.
Gee, maybe that’s why!! Doh. LOL shit happens
 

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ttocs

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ah yup I am sure you and I are not the only ones that have been in this place. lessons learned that you hopefully only do one time. I was having issues onetime where it was bucking under acceleration. I popped the hood and everything looked normal till I noticed there was a SLIGHT gap between the cold air intake and the upper/tb. It looked almost normal but you could pull it back just enough to where it was not making contact and well.... Never had that issue again.
 
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Daryl

Daryl

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Had looms on my ‘59 F100 but those wires were cut to fit. So, not sure the pre-cuts would be long enough to work.
The headers are BBK
 

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