Need help, wierd issues with 351

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GREG@SN95

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I bought a truck recently, a 91 f150 4x4 with a 302 and an m5od trans.. It was misfiring pretty bad when I got it, I didn't care though since I have several 302s laying around... Long story short, the knuckle head that owned the car before me must not known how to drive a stick... All the pushrods were bent and I think he over revved the thing...

Long story short, I got a screaming deal on a mercruiser 351 small block. This thing has under 100 hours, cast iron everything, stainless head gaskets, marine cam and double roller timing chain... Casting numbers read E6T so its an 86 truck motor.

The fuel mechanical fuel pump is new, as is the vac advance points distributor, and coil. I set the timing at 10 degrees before TDC (with the advance disconnected). I have the advance hooked straight to the metered vac port (no check valve). I solved a few issues after spending 5 hours learning about metered vac vs manifold vac and check valves and timing etc etc etc...

Now the carb is the only thing that isn't new. Its a 670cfm holley street avenger that I bought on ebay 2 years ago. It sat on a shelf for 2 years. The squirters on it were clogged and I halfway rebuilt the carb... I say halfway because the kit didn't come with a diaphragm or any thing else for the secondaries, just gaskets for the bowl.

Truck runs GREAT 99% of the time... Here is where it gets weird. Sometimes, while accelerating at like 5-10% throttle the motor bogs and backfires. Sometimes it doesn't. Last night it was running great... Then all the sudden it started running like shit. I thought it had a vacuum leak... But it did not. An hour later I start the truck and its fine...

What the fuck could cause this?
 
OP
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G

GREG@SN95

Guest
CC'S95GT said:
sticking choke on the carb?
what kind of dizzy?

No, choke is fine and motor warm when this happens...

Dizzy came off of a 1973 ford LTD that I was driving about 2 years ago. About 500 miles before I took that car off the road I replaced it. I think I bought the thing from autozone...

I replaced and gap'd the points at .017" and changed the condenser, cap and rotor...
 

All_Ford_Fun

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I use to have a 78 bronco with a 460 that done the same thing , one night while 4wheelin i crimped a tail pipe from getting high centered in 2 spots. When i went to fix it the next day i replaced the whole exhaust and changed my carb to an eledelbrock, I don't know if the holly was bad or if it was the exhaust but that fixed what ever it was
 

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