HawkX66
Member
There hasn't been a lot of
traffic at stangnet for SN95s, so I figured I'd give you guys a lookie see.
Here is what I've been up to. I picked up an 00 Mustang with a stock full
02 GT drive train. 4.6L, TR3650 & 8.8" 3.27 rear end. Almost
immediately I started getting a noise that sounded like valve train issues. I
opened the valve cover and it was a mess. Previous owner didn't believe in oil
changes apparently... So I threw a set of lash adjusters and plugs at it
along with new COP boots. They were smoked for sure and needed it. Still an
internal engine rattle it sounds like so I installed a Cloyes timing kit. Left
bank went in kind of tight, but it ran well after with the noise still. Overall
the engine quieted down a lot. I pulled the motor this past weekend and
stripped it to the short block. Nothing obviously wrong. I think I figured it
out and I hope it's as simple as I think it might be. After hot tanking the
motor or something similar, I'll be measuring everything and putting it back
together. Hopefully it was either an oil clog or something a lot more simple
that I think it might be.
If you guys think of anything else I should check, give me a holler please.
Here's some pics:
It's getting a cowl hood and both the hood and trunk will be flat black.
The first glimpses of the real ugliness...
traffic at stangnet for SN95s, so I figured I'd give you guys a lookie see.
Here is what I've been up to. I picked up an 00 Mustang with a stock full
02 GT drive train. 4.6L, TR3650 & 8.8" 3.27 rear end. Almost
immediately I started getting a noise that sounded like valve train issues. I
opened the valve cover and it was a mess. Previous owner didn't believe in oil
changes apparently... So I threw a set of lash adjusters and plugs at it
along with new COP boots. They were smoked for sure and needed it. Still an
internal engine rattle it sounds like so I installed a Cloyes timing kit. Left
bank went in kind of tight, but it ran well after with the noise still. Overall
the engine quieted down a lot. I pulled the motor this past weekend and
stripped it to the short block. Nothing obviously wrong. I think I figured it
out and I hope it's as simple as I think it might be. After hot tanking the
motor or something similar, I'll be measuring everything and putting it back
together. Hopefully it was either an oil clog or something a lot more simple
that I think it might be.
If you guys think of anything else I should check, give me a holler please.
Here's some pics:
It's getting a cowl hood and both the hood and trunk will be flat black.
The first glimpses of the real ugliness...